Hayter 21 project

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  • #43634
    past-timer
    Participant

    Well I got the Hayter fettled this morning, blades swinging, wheels spinning, belts tightened and nipples greased. I did perhaps 15mins easy cutting and then hit a rock in some nettles and now the machine won’t fire – I think the flywheel must have spun on the crank. Hey ho – easy enough to fix, and I was pleased with the cut and the speed

    #43636
    past-timer
    Participant

    Just to add, I found I could get enough of the distortion out of the cutter plate using a G clamp and a bit of something straight – I had a short bit of box section to hand

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    #43679
    past-timer
    Participant

    The flywheel had spun slightly. So I have now taken apart and reassembled with a new key, lapping the flywheel well and torquing it down with the rope in the bore trick to lock the crank, and the special clutch drive tool which I bought for the job.

    The mower was then running OK, but was difficult to start without pouring a little petrol into the carb – which pointed to the choke. With the air filter off, I sprayed some GT85 into the bowden cable and sprayed carb cleaner into the carb, and wiggled the control lever back and forward to make sure that the choke butterfly was flapping as it should do. It wasn’t at first, but was after a bit of attention. With that done and checking that the bowden cable was clamped in the right place, the mower starts, and I’ve been able to do some mowing. I’m really pleased – the machine is just what I need and I hope I can keep it going for a while now.

    I need to make a few parts that are missing – might anyone be able to send me close up photos of them?
    They are the wing nut that adjusts the height at the back, and the collar beneath it, and also the front wheel hub caps.

    thanks
    Matt

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    #43681
    past-timer
    Participant

    Rope in the bore enables locking of crank if you haven’t got the special flywheel holder and don’t want to risk breaking any fins off the flywheel. I rotated the engine so that the valves were closed, feed as much rope as I could into the bore and then turned the flywheel cw to feel it lock. I could then torque it to 60 ft lb.

    None of the soft keys I bought on ebay were a good fit – they needed dressing with a file first, and I had made sure the slots in the flywheel and on the crank, were really clean.

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